世界桥梁
世界橋樑
세계교량
WORLD BRIDGE
2015年
1期
88-92
,共5页
T形刚构桥%箱形梁%预应力偏位%顶板开裂%维修方案%应力%有限元法
T形剛構橋%箱形樑%預應力偏位%頂闆開裂%維脩方案%應力%有限元法
T형강구교%상형량%예응력편위%정판개렬%유수방안%응력%유한원법
T-shaped rigid-frame bridge%box girder%prestress deviation%top plate cracking%maintenance scheme%prestress%finite element method
某T形刚构桥在顶板预应力张拉过程中出现了箱内顶板混凝土崩裂病害,病害原因为混凝土强度不足和预应力定位偏差。针对该病害,提出顶板局部凿除方案(凿除崩裂区顶板,顺直管道后恢复)和顶板局部补强方案(新增横隔板),采用MI‐DAS建立该桥有限元模型,从施工难度和结构应力两方面进行比较分析,最后确定采用施工难度小、顶板压应力均匀且极值较小的局部补强方案作为推荐方案。采用减少预应力和增加铺装层厚度对推荐方案进行结构应力和主梁线形的优化,并对优化后维修方案进行施工阶段和成桥状态的结构验算。结果表明:结构各项验算指标均能满足规范要求,证明维修方案是合理的,通过维修可以保证桥梁的施工过程安全及使用要求。
某T形剛構橋在頂闆預應力張拉過程中齣現瞭箱內頂闆混凝土崩裂病害,病害原因為混凝土彊度不足和預應力定位偏差。針對該病害,提齣頂闆跼部鑿除方案(鑿除崩裂區頂闆,順直管道後恢複)和頂闆跼部補彊方案(新增橫隔闆),採用MI‐DAS建立該橋有限元模型,從施工難度和結構應力兩方麵進行比較分析,最後確定採用施工難度小、頂闆壓應力均勻且極值較小的跼部補彊方案作為推薦方案。採用減少預應力和增加鋪裝層厚度對推薦方案進行結構應力和主樑線形的優化,併對優化後維脩方案進行施工階段和成橋狀態的結構驗算。結果錶明:結構各項驗算指標均能滿足規範要求,證明維脩方案是閤理的,通過維脩可以保證橋樑的施工過程安全及使用要求。
모T형강구교재정판예응력장랍과정중출현료상내정판혼응토붕렬병해,병해원인위혼응토강도불족화예응력정위편차。침대해병해,제출정판국부착제방안(착제붕렬구정판,순직관도후회복)화정판국부보강방안(신증횡격판),채용MI‐DAS건립해교유한원모형,종시공난도화결구응력량방면진행비교분석,최후학정채용시공난도소、정판압응력균균차겁치교소적국부보강방안작위추천방안。채용감소예응력화증가포장층후도대추천방안진행결구응력화주량선형적우화,병대우화후유수방안진행시공계단화성교상태적결구험산。결과표명:결구각항험산지표균능만족규범요구,증명유수방안시합리적,통과유수가이보증교량적시공과정안전급사용요구。
T he deterioration of top plate concrete cracking occurred inside the box girder of a T‐shaped rigid‐frame bridge during the tensioning of the top plate prestressing tendons ,which was attributed to deficient concrete strength and prestress positioning deviation .In light of this deterio‐ration ,two schemes are proposed ,one is to locally remove the top plate ,that is ,to remove the cracked top plate and recast it after the prestressing ducts are straightened ;and the other is a local strengthening method ,namely to add diaphragms .MIDAS was used to establish the finite element model of the bridge to compare and analyze the two schemes from aspects of construction complexi‐ty and structural stress .As a result ,the local strengthening scheme which features low construc‐tion complexity ,uniform top plate compressive stress and smaller threshold value of compressive stress was determined as the recommended scheme .The recommended scheme was optimized in terms of structural stress and main girder geometry by reducing prestressing tendons and increas‐ing the thickness of deck pavement ,and the structure of the bridge during the construction process and in the completed bridge state was checked after the maintenance scheme was optimized .The results of the checking demonstrate that all the checking indexes of the structure could meet the code requirements ,proving that the maintenance scheme is rational .T he maintenance ensures that the bridge construction process is safe and its service condition meets the requirements .