绝缘材料
絕緣材料
절연재료
INSULATING MATERIALS
2015年
4期
69-72
,共4页
邱太洪%王俊波%李国伟%何胜红%黄育龙%刘少辉
邱太洪%王俊波%李國偉%何勝紅%黃育龍%劉少輝
구태홍%왕준파%리국위%하성홍%황육룡%류소휘
10 kV管型母线%红外测温%故障检测%局部放电
10 kV管型母線%紅外測溫%故障檢測%跼部放電
10 kV관형모선%홍외측온%고장검측%국부방전
10 kV tubular busbar%infrared temperature measurement%fault detection%partial discharge
针对某110 kV变电站10 kV变低管型母线在红外测温过程中2#主变B相变低管型母线出现测温异常的情况,采用常规停电方法测量具有一定的局限性,通过采用脉冲电流局放检测法及极性定位法查明缺陷原因,并解体进一步验证试验及分析结果。结果表明:10 kV管型母线的绝缘电阻、介质损耗及电容量、回路电阻等常规测试手段在绝缘受潮初期检测过程中具有一定的局限性,脉冲电流局放检测法能很好地弥补这些不足,可以在10 kV管型母线的检测中推广使用。
針對某110 kV變電站10 kV變低管型母線在紅外測溫過程中2#主變B相變低管型母線齣現測溫異常的情況,採用常規停電方法測量具有一定的跼限性,通過採用脈遲電流跼放檢測法及極性定位法查明缺陷原因,併解體進一步驗證試驗及分析結果。結果錶明:10 kV管型母線的絕緣電阻、介質損耗及電容量、迴路電阻等常規測試手段在絕緣受潮初期檢測過程中具有一定的跼限性,脈遲電流跼放檢測法能很好地瀰補這些不足,可以在10 kV管型母線的檢測中推廣使用。
침대모110 kV변전참10 kV변저관형모선재홍외측온과정중2#주변B상변저관형모선출현측온이상적정황,채용상규정전방법측량구유일정적국한성,통과채용맥충전류국방검측법급겁성정위법사명결함원인,병해체진일보험증시험급분석결과。결과표명:10 kV관형모선적절연전조、개질손모급전용량、회로전조등상규측시수단재절연수조초기검측과정중구유일정적국한성,맥충전류국방검측법능흔호지미보저사불족,가이재10 kV관형모선적검측중추엄사용。
In view of the abnormal situation of 2# main transformer B phase tubular busbar found in the infrared temperature measurement process of 10 kV tubular busbar in an 110 kV substation, because con-ventional outage measurement method has certain limitation, we used pulse current partial discharge detec-tion method and polar localization method to find the cause and further verified the test results by disas-sembly. The results show that the insulation resistance, dielectric loss and capacitance, loop resistance and other conventional test methods have some limitations in the early stage of insulation moistened, and the pulse current partial discharge detection method can remedy these shortcomings well, which can be ex-tended to use in detection of 10 kV tubular busbar.