水道港口
水道港口
수도항구
JOURNAL OF WATERWAY AND HARBOR
2015年
2期
140-144
,共5页
李琳%王梦婷%白兆亮%谭义海
李琳%王夢婷%白兆亮%譚義海
리림%왕몽정%백조량%담의해
底孔泄洪洞%悬栅式消能工%平底渐扩式消力池
底孔洩洪洞%懸柵式消能工%平底漸擴式消力池
저공설홍동%현책식소능공%평저점확식소력지
deep flood discharge tunnel%suspended grid energy dissipater%gradually expanding flat-bottom stilling basin
通过新疆青河县KYD水库底孔泄洪洞平底渐扩式消力池设计方案的试验,发现消力池池深、池长、边墙高远不能满足安全泄流要求。优化方案试验结果表明,对于渐扩角1.37°的渐扩式消力池按等宽度矩形消力池估算时池长基本满足要求,但是池深估算误差较大。联立溢洪道设计规范中的渐扩式消力池共轭水深计算公式和渐扩式消力池池深经验公式可较准确地计算池深。为了减小跃后水流剧烈脉动,降低跃后水深,采用了悬栅式消能工。试验结果表明,水跃淹没度增大,悬栅起到了破碎栅条上部水跃剧烈回旋运动引起的表面漩滚,消力池内水深降低,最大水深减小1.0 m,陡坡段和消力内水流脉动明显减弱,浪花溅起高度明显小于加悬栅前。
通過新疆青河縣KYD水庫底孔洩洪洞平底漸擴式消力池設計方案的試驗,髮現消力池池深、池長、邊牆高遠不能滿足安全洩流要求。優化方案試驗結果錶明,對于漸擴角1.37°的漸擴式消力池按等寬度矩形消力池估算時池長基本滿足要求,但是池深估算誤差較大。聯立溢洪道設計規範中的漸擴式消力池共軛水深計算公式和漸擴式消力池池深經驗公式可較準確地計算池深。為瞭減小躍後水流劇烈脈動,降低躍後水深,採用瞭懸柵式消能工。試驗結果錶明,水躍淹沒度增大,懸柵起到瞭破碎柵條上部水躍劇烈迴鏇運動引起的錶麵漩滾,消力池內水深降低,最大水深減小1.0 m,陡坡段和消力內水流脈動明顯減弱,浪花濺起高度明顯小于加懸柵前。
통과신강청하현KYD수고저공설홍동평저점확식소력지설계방안적시험,발현소력지지심、지장、변장고원불능만족안전설류요구。우화방안시험결과표명,대우점확각1.37°적점확식소력지안등관도구형소력지고산시지장기본만족요구,단시지심고산오차교대。련립일홍도설계규범중적점확식소력지공액수심계산공식화점확식소력지지심경험공식가교준학지계산지심。위료감소약후수류극렬맥동,강저약후수심,채용료현책식소능공。시험결과표명,수약엄몰도증대,현책기도료파쇄책조상부수약극렬회선운동인기적표면선곤,소력지내수심강저,최대수심감소1.0 m,두파단화소력내수류맥동명현감약,랑화천기고도명현소우가현책전。
Through the test of design scheme for the gradually expanding flat?bottom stilling basin deep flood discharge tunnel of KYD Reservoir in Green River county in Xinjiang, it is found that length, depth and sidewall height can not meet the security requirements. The design scheme shows that:the length of stilling basin basically meets the requirements of the stilling basin with the divergent angle of 1.37°,when estimates according to stilling ba?sin which is equal width and rectangle, but estimated error is large. The formula of conjugate depth of gradually ex?panding stilling basin was combined with the empirical formula of width of gradually expanding stilling basin to cal?culate the width directly. Suspended grid energy dissipater was used to decrease intense pulsating water and se?quent depth. The results show that the surface eddies which caused by upper water jump intense cyclotron motion are broken with the increase of submergence degree. What is more, the maximum depth in stilling basin decreases by 1 m. Flow pulsation reduces significantly, and the height of waves splashing is significantly less than before.