南方电网技术
南方電網技術
남방전망기술
SOUTHERN POWER SYSTEM TECHNOLOGY
2015年
3期
28-30
,共3页
李标俊%郭琦%贾旭东%刘涛
李標俊%郭琦%賈旭東%劉濤
리표준%곽기%가욱동%류도
直流输电%直流线路纵差保护%实时数字仿真系统%高阻抗接地故障
直流輸電%直流線路縱差保護%實時數字倣真繫統%高阻抗接地故障
직류수전%직류선로종차보호%실시수자방진계통%고조항접지고장
HVDC transmission%DC line longitudinal differential protection%RTDS%high impedance ground fault
结合一起兴安直流线路因高阻接地故障引起的跳闸事故,通过对87DCLL逻辑的分析,对兴安直流线路纵差保护原理进行了改进。提出将87DCLL去掉“600 ms闭锁逻辑”,并基于仿真结果将保护延时调整至800 ms。仿真结果验证了所提措施不会导致87DCLL出现误动,并且在直流线路发生高阻抗接地故障时87DCLL能正确动作。
結閤一起興安直流線路因高阻接地故障引起的跳閘事故,通過對87DCLL邏輯的分析,對興安直流線路縱差保護原理進行瞭改進。提齣將87DCLL去掉“600 ms閉鎖邏輯”,併基于倣真結果將保護延時調整至800 ms。倣真結果驗證瞭所提措施不會導緻87DCLL齣現誤動,併且在直流線路髮生高阻抗接地故障時87DCLL能正確動作。
결합일기흥안직류선로인고조접지고장인기적도갑사고,통과대87DCLL라집적분석,대흥안직류선로종차보호원리진행료개진。제출장87DCLL거도“600 ms폐쇄라집”,병기우방진결과장보호연시조정지800 ms。방진결과험증료소제조시불회도치87DCLL출현오동,병차재직류선로발생고조항접지고장시87DCLL능정학동작。
Based on analysis of a tripping accident in Xing-An HVDC system due to high impedance ground fault and the logic of 87DCLL, this paper presents an improvement of the DC line longitudinal differential protection principle. It is proposed to remove the"600 ms blocking logic" from 87DCLL, and adjust the delay to 800 ms based on simulation results. Simulation results demenstrate that the proposed measures would not lead to 87DCLL malfunction, and 87DCLL can operate correctly when a high-impedance ground fault occurs in the DC line .