水利与建筑工程学报
水利與建築工程學報
수리여건축공정학보
TECHNIQUE OF SEEPAGE CONTROL
2015年
4期
183-187,219
,共6页
宾斌%蒋厚良%王雪龙%赵铁军
賓斌%蔣厚良%王雪龍%趙鐵軍
빈빈%장후량%왕설룡%조철군
导水布袋%布袋注浆%软土地基%淤泥质土%加固处理
導水佈袋%佈袋註漿%軟土地基%淤泥質土%加固處理
도수포대%포대주장%연토지기%어니질토%가고처리
drainage bag%bag grouting%soft soil foundation%silt soil%reinforcement
为更有效地对软土质堤防进行加固处理,将布袋注浆技术和可控性压密注浆桩技术融为一个整体,形成一项新的软土地基处理技术———导水布袋复合压密注浆桩技术。该技术利用布袋的良好导水性,有效解决了软土在压密注浆处理过程中,超孔隙水压力消散过慢的技术难题。将导水布袋复合压密注浆桩技术应用于洞庭湖软土质堤防加固试验处理,通过对处理前后的原状土进行标准贯入试验,对桩和桩间土进行取芯检测以及施工结束后位移观测、现场回访等,分析论证了导水布袋复合压密注浆桩技术对软土质堤防的加固效果。在加固处理一年后,监测结果表明,堤防侧向位移量趋于收敛,堤基已处于稳定状态。
為更有效地對軟土質隄防進行加固處理,將佈袋註漿技術和可控性壓密註漿樁技術融為一箇整體,形成一項新的軟土地基處理技術———導水佈袋複閤壓密註漿樁技術。該技術利用佈袋的良好導水性,有效解決瞭軟土在壓密註漿處理過程中,超孔隙水壓力消散過慢的技術難題。將導水佈袋複閤壓密註漿樁技術應用于洞庭湖軟土質隄防加固試驗處理,通過對處理前後的原狀土進行標準貫入試驗,對樁和樁間土進行取芯檢測以及施工結束後位移觀測、現場迴訪等,分析論證瞭導水佈袋複閤壓密註漿樁技術對軟土質隄防的加固效果。在加固處理一年後,鑑測結果錶明,隄防側嚮位移量趨于收斂,隄基已處于穩定狀態。
위경유효지대연토질제방진행가고처리,장포대주장기술화가공성압밀주장장기술융위일개정체,형성일항신적연토지기처리기술———도수포대복합압밀주장장기술。해기술이용포대적량호도수성,유효해결료연토재압밀주장처리과정중,초공극수압력소산과만적기술난제。장도수포대복합압밀주장장기술응용우동정호연토질제방가고시험처리,통과대처리전후적원상토진행표준관입시험,대장화장간토진행취심검측이급시공결속후위이관측、현장회방등,분석론증료도수포대복합압밀주장장기술대연토질제방적가고효과。재가고처리일년후,감측결과표명,제방측향위이량추우수렴,제기이처우은정상태。
In order to reinforce soft soil embankment more effectively ,bag grouting and controllable pressure grouting pile technique were combined to develop a new treatment measure of soft soil foundation ,namly ,condensed grouting pile with drainage bag lining .With this technique ,the favorable hydraulic conductivity of the cloth bags was taken advantage of to solve the problems of slow pore water pressure dissipation in the grouting process of soft soil .Here this technique was adopted in the reinforcement treatment test of Dongting lake soft soil embankment .Based on the standard penetration tests of the undisturbed soil before and after the treatment ,the detection of core soil of the pile and between the piles ,as well as the displacement observation and site investigation after the construction was completed , the reinforcement effect of condensed grouting pile with drainage bag lining technique was analyzed and demonstrated .One year after the reinforce-ment ,the monitoring results of the embankment indicate that the literal displacement is diminishing ,the foundation of the embankment is stable .