油气藏评价与开发
油氣藏評價與開髮
유기장평개여개발
2015年
4期
64-68
,共5页
范落成%王杰东%何小明%胡林
範落成%王傑東%何小明%鬍林
범락성%왕걸동%하소명%호림
KCl%聚磺钻井液%抑制性%高温稳定性%TP338H井
KCl%聚磺鑽井液%抑製性%高溫穩定性%TP338H井
KCl%취광찬정액%억제성%고온은정성%TP338H정
KCl%polysulfonate drilling fluid%inhibition%high temperature stability%well TP338H
在TP338H井的几口邻井施工时,三开井段均采用常规聚磺钻井液体系,在钻井过程中,PDC钻头泥包、井壁失稳垮塌、下钻大段划眼等复杂情况时有发生,严重影响了钻井施工进度。通过查询和调研相关钻井液资料,决定在TP338H井三开使用KCl聚磺钻井液体系,以聚磺钻井液为基础,通过加入KCl来增强其抑制性和防塌性能。室内性能评价表明,KCl聚磺钻井液的抑制防塌性、高温稳定性、抗污染性、润滑性及流变性能均优于常规聚磺钻井液体系。该井三开井段施工顺利,未出现钻头泥包、严重垮塌等复杂情况,KCl聚磺钻井液体系在该井取得了良好的应用效果,对以后该区块的钻井液施工具有很好的参考意义。
在TP338H井的幾口鄰井施工時,三開井段均採用常規聚磺鑽井液體繫,在鑽井過程中,PDC鑽頭泥包、井壁失穩垮塌、下鑽大段劃眼等複雜情況時有髮生,嚴重影響瞭鑽井施工進度。通過查詢和調研相關鑽井液資料,決定在TP338H井三開使用KCl聚磺鑽井液體繫,以聚磺鑽井液為基礎,通過加入KCl來增彊其抑製性和防塌性能。室內性能評價錶明,KCl聚磺鑽井液的抑製防塌性、高溫穩定性、抗汙染性、潤滑性及流變性能均優于常規聚磺鑽井液體繫。該井三開井段施工順利,未齣現鑽頭泥包、嚴重垮塌等複雜情況,KCl聚磺鑽井液體繫在該井取得瞭良好的應用效果,對以後該區塊的鑽井液施工具有很好的參攷意義。
재TP338H정적궤구린정시공시,삼개정단균채용상규취광찬정액체계,재찬정과정중,PDC찬두니포、정벽실은과탑、하찬대단화안등복잡정황시유발생,엄중영향료찬정시공진도。통과사순화조연상관찬정액자료,결정재TP338H정삼개사용KCl취광찬정액체계,이취광찬정액위기출,통과가입KCl래증강기억제성화방탑성능。실내성능평개표명,KCl취광찬정액적억제방탑성、고온은정성、항오염성、윤활성급류변성능균우우상규취광찬정액체계。해정삼개정단시공순리,미출현찬두니포、엄중과탑등복잡정황,KCl취광찬정액체계재해정취득료량호적응용효과,대이후해구괴적찬정액시공구유흔호적삼고의의。
In the construction of adjacent wells of well TP338H, the third drilling sections all adopted the conventional polysulfo?nate drilling fluid. In the process of drilling, some complex situations often occurred, including PDC bit balling, wellbore instability and long section reaming, which affected the drilling construction schedule seriously. Through researching the related materials of drilling fluid, in the third drilling of well TP338H, KCl polysulfonate drilling fluid system was adopted. Using polysulfonate drilling fluid as the foundation, the inhibition and anti collapse properties were enhanced by adding KCl. The indoor results show that, the performances of KCl polysulfonate drilling fluid system are superior to those of conventional polysulfonate drilling fluid system, among them, the performances include inhibition and anti collapse, high temperature stability, anti pollution ability, lubricity and rheological properties. The third drilling construction of this well was smooth, and the complex situations including bit balling and serious collapse were not happened. KCl polysulfonate drilling fluid system achieves good results in the well, thereby offering good references for future construction in this block.