当代化工
噹代化工
당대화공
Contemporary Chemical Industry
2015年
10期
2403-2405
,共3页
蒋旭%宋传阳%张侃毅%刘景宇
蔣旭%宋傳暘%張侃毅%劉景宇
장욱%송전양%장간의%류경우
超稠油%SAGD 采出液%高温密闭脱水%耐温破乳剂
超稠油%SAGD 採齣液%高溫密閉脫水%耐溫破乳劑
초주유%SAGD 채출액%고온밀폐탈수%내온파유제
Super heavy oil%SAGD produced fluid%High temperature sealed dehydration%Demulsifier
随着新疆风城超稠油规模开发,SAGD 开发方式被广泛用于油田生产,该部分采出液进入常规稠油处理站后,造成原油脱水困难,并导致出水指标恶化,给油水处理系统的平稳运行造成很大冲击。为解决 SAGD采出液油水处理难题,CPE 新疆设计院通过大量室内研究和动态模拟试验,初步确定了“气液分离、高效预脱水、高温正向破乳”的 SAGD 采出液高温密闭处理流程,辅以“预脱水剂、正向破乳剂”的药剂体系,以确保SAGD 采出液在低粘度、高密度差的最佳工况下实现油水高效分离。根据风城油田30×104 t/a 规模 SAGD 采出液处理站建站初期现场试验情况,通过试验数据分析,对室内研究结果进行工业化验证,同时为该站生产运行提供数据支持。
隨著新疆風城超稠油規模開髮,SAGD 開髮方式被廣汎用于油田生產,該部分採齣液進入常規稠油處理站後,造成原油脫水睏難,併導緻齣水指標噁化,給油水處理繫統的平穩運行造成很大遲擊。為解決 SAGD採齣液油水處理難題,CPE 新疆設計院通過大量室內研究和動態模擬試驗,初步確定瞭“氣液分離、高效預脫水、高溫正嚮破乳”的 SAGD 採齣液高溫密閉處理流程,輔以“預脫水劑、正嚮破乳劑”的藥劑體繫,以確保SAGD 採齣液在低粘度、高密度差的最佳工況下實現油水高效分離。根據風城油田30×104 t/a 規模 SAGD 採齣液處理站建站初期現場試驗情況,通過試驗數據分析,對室內研究結果進行工業化驗證,同時為該站生產運行提供數據支持。
수착신강풍성초주유규모개발,SAGD 개발방식피엄범용우유전생산,해부분채출액진입상규주유처리참후,조성원유탈수곤난,병도치출수지표악화,급유수처리계통적평은운행조성흔대충격。위해결 SAGD채출액유수처리난제,CPE 신강설계원통과대량실내연구화동태모의시험,초보학정료“기액분리、고효예탈수、고온정향파유”적 SAGD 채출액고온밀폐처리류정,보이“예탈수제、정향파유제”적약제체계,이학보SAGD 채출액재저점도、고밀도차적최가공황하실현유수고효분리。근거풍성유전30×104 t/a 규모 SAGD 채출액처리참건참초기현장시험정황,통과시험수거분석,대실내연구결과진행공업화험증,동시위해참생산운행제공수거지지。
With scale development of Fengcheng super heavy oil in Xinjiang Oilfield, SAGD development mode has been widely used in oilfield production. In the production, part of the produced fluid is piped to the 1st heavy oil treatment station, which can result in the difficulty of crude oil dehydration in the station to make the sedimentation tank effluent index worse, to cause great impact on the smooth operation of water treatment system. In order to solve the water treatment problems, through experimental research and dynamic simulation, Xinjiang institute initially established a high temperature sealed dehydration process of "gas-liquid separation, efficient pre-dehydration and high temperature demulsification", supplemented by "pre-dehydrating agent and demulsifier" the agent system. The process can ensure efficient separation of oil and water in SAGD produced fluid under optimum conditions. In this paper, based on field test of 30×104 t/a SAGD produced liquid treatment station, through test data analysis, industrial test of the process was carried out.