空军工程大学学报(自然科学版)
空軍工程大學學報(自然科學版)
공군공정대학학보(자연과학판)
Journal of Air Force Engineering University (Natural Science Edition)
2015年
5期
93-95
,共3页
李其轩%于洪江%张晓义%唐志强
李其軒%于洪江%張曉義%唐誌彊
리기헌%우홍강%장효의%당지강
沥青路面%路况评价%破损面积%蒙特卡洛仿真
瀝青路麵%路況評價%破損麵積%矇特卡洛倣真
력청로면%로황평개%파손면적%몽특잡락방진
asphalt pavement%current maintenance standard%pavement condition evaluation%damage area
针对现行规范中对沥青路面破损面积的评定不够明确等问题,提出修补宽度达到路段宽度时不应参与路面破损状况评价,重新选取修补损坏面积换算系数(K )为0.7;提出一种基于蒙特卡洛算法的 Matlab 检验方法对 K =0.7的合理性进行了检验,先将已有数据输入 Mat-lab 分布拟合,得出影响路况指数(PCI)的修补面积、裂缝总长度、其他破损面积等因素服从的分布函数,进而使用蒙特卡洛算法模拟得出大量数据,计算相应的 PCI,得出路况评价结果。最后通过与实际路况比较和实际工程应用进行检验,证明了 K 取0.7可以得到合理的统计计算破损面积方法。
針對現行規範中對瀝青路麵破損麵積的評定不夠明確等問題,提齣脩補寬度達到路段寬度時不應參與路麵破損狀況評價,重新選取脩補損壞麵積換算繫數(K )為0.7;提齣一種基于矇特卡洛算法的 Matlab 檢驗方法對 K =0.7的閤理性進行瞭檢驗,先將已有數據輸入 Mat-lab 分佈擬閤,得齣影響路況指數(PCI)的脩補麵積、裂縫總長度、其他破損麵積等因素服從的分佈函數,進而使用矇特卡洛算法模擬得齣大量數據,計算相應的 PCI,得齣路況評價結果。最後通過與實際路況比較和實際工程應用進行檢驗,證明瞭 K 取0.7可以得到閤理的統計計算破損麵積方法。
침대현행규범중대력청로면파손면적적평정불구명학등문제,제출수보관도체도로단관도시불응삼여로면파손상황평개,중신선취수보손배면적환산계수(K )위0.7;제출일충기우몽특잡락산법적 Matlab 검험방법대 K =0.7적합이성진행료검험,선장이유수거수입 Mat-lab 분포의합,득출영향로황지수(PCI)적수보면적、렬봉총장도、기타파손면적등인소복종적분포함수,진이사용몽특잡락산법모의득출대량수거,계산상응적 PCI,득출로황평개결과。최후통과여실제로황비교화실제공정응용진행검험,증명료 K 취0.7가이득도합리적통계계산파손면적방법。
Aimed at the problems that evaluation of pavement damage area in current standards is not clear enough,a current asphalt pavement condition evaluation model is introduced.If the repair area width rea-ches the pavement width,this should not be involved in pavement damage condition evaluation.Conversion coefficient K of repairing damage area should be 0.7.A Matlab testing method based on Mandonte Carlo al-gorithm is put forward to examine the rationality of K being 0.7.The concrete conditions are as follows:First,input the known data to Matlab to fit,and then,derive the functions of elements obey affected pavement condition index,such as repair area,total crack length and other damage areas,etc.,Last,cal-culate the corresponding PCI to get the result of pavement condition evaluation by using Monte Carlo algo-rithm.Through the comparison with the actual pavement conditions and the actual test,the rationality of K being 0.7 is verified.