流体机械
流體機械
류체궤계
Fluid Machinery
2015年
9期
10-14,87
,共6页
周恩民%程松%张文%刘恺%熊波%王仪田%施宏博%程超
週恩民%程鬆%張文%劉愷%熊波%王儀田%施宏博%程超
주은민%정송%장문%류개%웅파%왕의전%시굉박%정초
连续式风洞%驻室抽气%离心式压缩机%性能测试
連續式風洞%駐室抽氣%離心式壓縮機%性能測試
련속식풍동%주실추기%리심식압축궤%성능측시
continuous wind tunnel%plenum suction system%centrifugal compressor%performance test
为了研究驻室抽气压缩机及其与风洞性能的相关性,对 E71-3离心压缩机进行了性能试验,并进行了驻室抽气性能测试。试验结果表明:(1)E71-3离心压缩机实测最高压比4.516,设计点多变效率81.8%,达到了设计要求。(2)风洞运行总压升高,压缩机多变效率降低。(3)风洞试验段 Ma =0.9~1.1时,驻室抽气量对风洞模型区梯度的影响不大,但驻室抽气量超过4%后风洞马赫数均方根偏差明显增大;压缩机稳定在中等转速、适量抽气量的工况,且入口流量调节阀全开,风洞流场品质较好,运行成本最低。
為瞭研究駐室抽氣壓縮機及其與風洞性能的相關性,對 E71-3離心壓縮機進行瞭性能試驗,併進行瞭駐室抽氣性能測試。試驗結果錶明:(1)E71-3離心壓縮機實測最高壓比4.516,設計點多變效率81.8%,達到瞭設計要求。(2)風洞運行總壓升高,壓縮機多變效率降低。(3)風洞試驗段 Ma =0.9~1.1時,駐室抽氣量對風洞模型區梯度的影響不大,但駐室抽氣量超過4%後風洞馬赫數均方根偏差明顯增大;壓縮機穩定在中等轉速、適量抽氣量的工況,且入口流量調節閥全開,風洞流場品質較好,運行成本最低。
위료연구주실추기압축궤급기여풍동성능적상관성,대 E71-3리심압축궤진행료성능시험,병진행료주실추기성능측시。시험결과표명:(1)E71-3리심압축궤실측최고압비4.516,설계점다변효솔81.8%,체도료설계요구。(2)풍동운행총압승고,압축궤다변효솔강저。(3)풍동시험단 Ma =0.9~1.1시,주실추기량대풍동모형구제도적영향불대,단주실추기량초과4%후풍동마혁수균방근편차명현증대;압축궤은정재중등전속、괄량추기량적공황,차입구류량조절벌전개,풍동류장품질교호,운행성본최저。
In order to study the compressor used in plenum suction system and it’s corelation with the wind tunnel perform-ance,the performance test of the E71 -3 centrifugal compressor and the plenum suction system were conducted.The maximal pressure ratio of the compressor measured in the test is 4.516 and the polytropic efficiency of the design point is 81.8% which have all achieved the design requirements.The compressor’s polytropic efficiency will decrease as the settling chamber total pressure increase.From Ma0.9 to Ma1.1 in wind tunnel test section,the plenum suction mass flow rate has a little effect on the gradient of the Mach number in the wind tunnel model area,the root-mean-square error will increase significantly if the plenum suction mass flow rate more than 4%,the wind tunnel flow quality will be well and the total running power will be lowest when the compressor’s rotation and the plenum suction mass flow rate at middle level,and the entrance air flow adjusting valve is fully opened.