石油钻采工艺
石油鑽採工藝
석유찬채공예
Oil Drilling & Production Technology
2015年
5期
113-115
,共3页
连续油管%沥青质%异常高压%硫化氢%井下作业%沥青质沉淀溶剂
連續油管%瀝青質%異常高壓%硫化氫%井下作業%瀝青質沉澱溶劑
련속유관%력청질%이상고압%류화경%정하작업%력청질침정용제
coiled tubing%asphaltene%abnormal high pressure%H2S%downhole operation%asphaltene precipitation solvent
两伊边界轻质油油田主力产层A油组在生产过程中,沥青质在井筒析出、沉淀的现象很严重,是无水开采阶段影响油井生产时率的主要因素之一。A油组异常高压,地层原油中高含硫化氢,所以整个作业过程,油管和油套环空之间不允许建立循环,这些都给井筒沥青质沉淀清除工作带来了很大困难。本次施工先采用泵车小排量控压、分段挤入、分段浸泡以及分段返排的工艺,挤入过程中井筒被沥青沉淀堵死,之后改用连续油管通洗井和泵车小排量控压挤入与浸泡相结合的工艺,顺利完成作业,使油井恢复正常生产。本次作业历时5 d,现场施工过程艰难复杂,通过作业认识到高效的沥青质沉淀溶剂、连续油管通洗、泵车控压控排量挤入、浸泡时间和浸泡深度几方面紧密配合是保证施工成功的关键。
兩伊邊界輕質油油田主力產層A油組在生產過程中,瀝青質在井筒析齣、沉澱的現象很嚴重,是無水開採階段影響油井生產時率的主要因素之一。A油組異常高壓,地層原油中高含硫化氫,所以整箇作業過程,油管和油套環空之間不允許建立循環,這些都給井筒瀝青質沉澱清除工作帶來瞭很大睏難。本次施工先採用泵車小排量控壓、分段擠入、分段浸泡以及分段返排的工藝,擠入過程中井筒被瀝青沉澱堵死,之後改用連續油管通洗井和泵車小排量控壓擠入與浸泡相結閤的工藝,順利完成作業,使油井恢複正常生產。本次作業歷時5 d,現場施工過程艱難複雜,通過作業認識到高效的瀝青質沉澱溶劑、連續油管通洗、泵車控壓控排量擠入、浸泡時間和浸泡深度幾方麵緊密配閤是保證施工成功的關鍵。
량이변계경질유유전주력산층A유조재생산과정중,력청질재정통석출、침정적현상흔엄중,시무수개채계단영향유정생산시솔적주요인소지일。A유조이상고압,지층원유중고함류화경,소이정개작업과정,유관화유투배공지간불윤허건립순배,저사도급정통력청질침정청제공작대래료흔대곤난。본차시공선채용빙차소배량공압、분단제입、분단침포이급분단반배적공예,제입과정중정통피력청침정도사,지후개용련속유관통세정화빙차소배량공압제입여침포상결합적공예,순리완성작업,사유정회복정상생산。본차작업력시5 d,현장시공과정간난복잡,통과작업인식도고효적력청질침정용제、련속유관통세、빙차공압공배량제입、침포시간화침포심도궤방면긴밀배합시보증시공성공적관건。
During production of the major productive zone-Oil Reservoir A in light oil oilifeld close to Iran and Iraq borders, asphaltene precipitation and settling in wellbore is a severe problems and is one of the factors which affect the production time efifciency of oil wells in water-free production period. The Oil Reservoir A has anomalously high pressure and formation crude oil contains large amount of hydrogen sulphide (H2S), so no circulation should be established between the tubing and casing annulus during the operation process. All these factors pose great dififculty for removing the asphaltene precipitation on wellbore. In this job, the pumping unit was ifrstly used to control the pressure with small displacement, squeeze in lfuid in stages and soak in stages and lfow back in stages. During squeezing, the wellbore was fully blocked by asphaltene precipitation.Then coiled tubing was used to drift and wash the well in conjunction with controlling the pressure by pumping unit with small displacement and soaking. The job was completed successfully and the oil well resumed normal production. This job lasted 5 days and experienced very dififcult and complex times. From the job, it is learned that close combination of efifcient asphaltene precipitation solvent, drifting by coiled tubing, squeezing by pumping unit with controlled pressure and displacement, soaking duration and soaking depth is the key to the success of the job.