非常规油气
非常規油氣
비상규유기
Unconventional Oil & Gas
2015年
3期
78-82
,共5页
气田开发%弹性能量指数%火山岩气藏%长岭气田
氣田開髮%彈性能量指數%火山巖氣藏%長嶺氣田
기전개발%탄성능량지수%화산암기장%장령기전
gas field development%elastic energy index%volcanic gas reservoir%Changling Gas Field
长岭气田营城组火山岩气藏开发中水侵速度及产量递减快, 需要分析气藏目前开发状况与稳产基础受损情况, 为气藏下步开发调整提供基础数据和理论依据. 结合气藏静态储层认识与开发动态特征, 利用气田动态分析方法, 从气藏弹性能量指数入手, 分析了气藏的开发特点、 气藏水侵、 气藏开发现状及下步研究及攻关方向, 明确季节性调峰措施是引起目前水侵的主要原因, 其本质是生产压差偏大导致气水平衡破坏而引起气藏快速水侵, 但气藏整体没有受到较大的破坏性影响, 仍具备一定时期的稳产能力. 建议该气藏下步开展有针对性的气藏描述和排水采气的先导试验, 并超前开展气藏调整方案的研究与编制工作, 使气藏真正实现科学合理开发.
長嶺氣田營城組火山巖氣藏開髮中水侵速度及產量遞減快, 需要分析氣藏目前開髮狀況與穩產基礎受損情況, 為氣藏下步開髮調整提供基礎數據和理論依據. 結閤氣藏靜態儲層認識與開髮動態特徵, 利用氣田動態分析方法, 從氣藏彈性能量指數入手, 分析瞭氣藏的開髮特點、 氣藏水侵、 氣藏開髮現狀及下步研究及攻關方嚮, 明確季節性調峰措施是引起目前水侵的主要原因, 其本質是生產壓差偏大導緻氣水平衡破壞而引起氣藏快速水侵, 但氣藏整體沒有受到較大的破壞性影響, 仍具備一定時期的穩產能力. 建議該氣藏下步開展有針對性的氣藏描述和排水採氣的先導試驗, 併超前開展氣藏調整方案的研究與編製工作, 使氣藏真正實現科學閤理開髮.
장령기전영성조화산암기장개발중수침속도급산량체감쾌, 수요분석기장목전개발상황여은산기출수손정황, 위기장하보개발조정제공기출수거화이론의거. 결합기장정태저층인식여개발동태특정, 이용기전동태분석방법, 종기장탄성능량지수입수, 분석료기장적개발특점、 기장수침、 기장개발현상급하보연구급공관방향, 명학계절성조봉조시시인기목전수침적주요원인, 기본질시생산압차편대도치기수평형파배이인기기장쾌속수침, 단기장정체몰유수도교대적파배성영향, 잉구비일정시기적은산능력. 건의해기장하보개전유침대성적기장묘술화배수채기적선도시험, 병초전개전기장조정방안적연구여편제공작, 사기장진정실현과학합리개발.
For high velocity of water invasion and sharp decline of production in gas reservoir development of Yingcheng Formation in Changling Gas Field, development and damage to stable production of gas reservoir was analyzed to provide basic research results and theoretical basis for next development. With perception of static reservoir feature and dynamic development feature, based on dynamic analysis, in particular, starting from elastic energy index reflecting the maintaining status of gas reservoir, development characteristics, influence of water invasion, current state and further research on reser-voir development were analyzed and discussed. It was confirmed that seasonal peak shaving measures were main causes of water invasion, and its essence was the destruction of the balance between gas and water caused by large production pres-sure difference, which led to rapid water invasion of gas reservoir. However, the gas reservoir as a whole was not affected by the destruction;even it had a certain period of stable capability. It was suggested that the pilot test of the gas reservoir with targeted gas reservoir description and drainage gas recovery be the next step, and positive research and formulation of gas reservoir adjustment scheme be carried out, so as to truly realize scientific and reasonable development of gas res-ervoir.