铁道学报
鐵道學報
철도학보
Journal of the China Railway Society
2015年
11期
110-116
,共7页
岩溶隧道%二次衬砌%水压特征%长期监测%理论分析
巖溶隧道%二次襯砌%水壓特徵%長期鑑測%理論分析
암용수도%이차츤체%수압특정%장기감측%이론분석
karst tunnel%second lining%water pressure character%long term monitoring%theory analysis
通过长期监测宜万铁路4座典型高风险岩溶隧道运营期衬砌水压,结合模型试验、理论分析研究岩溶隧道二次衬砌水压的特征,提出岩溶隧道衬砌水压计算的概化模型。研究表明:(1)各隧道实测衬砌水压总体值不大,最大0.13 MPa,低于1 MPa抗水压衬砌设计值;断面水压分布受洞内排水效应影响明显;水压的动态与雨季关系密切。(2)岩溶隧道初始水压的确定主要受隧道上、下方的排泄基准面控制,施工过程中的泄水洞构成新的排泄基准面;初始水压与排泄能力和降雨的补给有关。(3)只有考虑隧道排水时才能发挥注浆加固圈对渗透水压的衰减作用;二衬水压受隧道排水量Q2与渗入初期支护的水量Q1的综合影响,二次衬砌上水压与Q2/Q1成反比。(4)排水洞排水通畅对二衬水压影响较大,在运营的过程中,应对排水洞进行定期的检查和维护,保证其排水通畅。本文可为高水压岩溶隧道的设计与运营提供参考。
通過長期鑑測宜萬鐵路4座典型高風險巖溶隧道運營期襯砌水壓,結閤模型試驗、理論分析研究巖溶隧道二次襯砌水壓的特徵,提齣巖溶隧道襯砌水壓計算的概化模型。研究錶明:(1)各隧道實測襯砌水壓總體值不大,最大0.13 MPa,低于1 MPa抗水壓襯砌設計值;斷麵水壓分佈受洞內排水效應影響明顯;水壓的動態與雨季關繫密切。(2)巖溶隧道初始水壓的確定主要受隧道上、下方的排洩基準麵控製,施工過程中的洩水洞構成新的排洩基準麵;初始水壓與排洩能力和降雨的補給有關。(3)隻有攷慮隧道排水時纔能髮揮註漿加固圈對滲透水壓的衰減作用;二襯水壓受隧道排水量Q2與滲入初期支護的水量Q1的綜閤影響,二次襯砌上水壓與Q2/Q1成反比。(4)排水洞排水通暢對二襯水壓影響較大,在運營的過程中,應對排水洞進行定期的檢查和維護,保證其排水通暢。本文可為高水壓巖溶隧道的設計與運營提供參攷。
통과장기감측의만철로4좌전형고풍험암용수도운영기츤체수압,결합모형시험、이론분석연구암용수도이차츤체수압적특정,제출암용수도츤체수압계산적개화모형。연구표명:(1)각수도실측츤체수압총체치불대,최대0.13 MPa,저우1 MPa항수압츤체설계치;단면수압분포수동내배수효응영향명현;수압적동태여우계관계밀절。(2)암용수도초시수압적학정주요수수도상、하방적배설기준면공제,시공과정중적설수동구성신적배설기준면;초시수압여배설능력화강우적보급유관。(3)지유고필수도배수시재능발휘주장가고권대삼투수압적쇠감작용;이츤수압수수도배수량Q2여삼입초기지호적수량Q1적종합영향,이차츤체상수압여Q2/Q1성반비。(4)배수동배수통창대이츤수압영향교대,재운영적과정중,응대배수동진행정기적검사화유호,보증기배수통창。본문가위고수압암용수도적설계여운영제공삼고。
In this paper,based on long term tunnel lining water pressure monitoring for 4 typical high-risk karst tunnels in Yi-Wan railway line,the character of water pressure on the second lining of the karst tunnels was studied,together with model test and theory analysis.A generalized model for karst tunnel was put up to esti-mate water pressure on the second lining.The study showed:(1)The overall level of the measured water pres-sure on the second lining of each tunnel was low with the maximum of 0.13 MPa,far below 1 MPa,the design value of water pressure resistant lining .The distribution of water pressure of the cross section was significant-ly affected by tunnel drainage,while water pressure dynamic was closely related with rainy season.(2)The de-termination of the original water pressure of karst tunnel was controlled by drainage base level on or under the tunnel.The original water pressure was also related with drainage capacity and rainfall replenishment.The re-lease tunnel during construction formed the new drainage base level.(3)Only when there is drainage in tunnel, can the grouting reinforcement circle play the role of reducing water pressure on the lining.The water pressure on the second lining,inversely proportional to tunnel drainage(Q2 )and water seepage into the primary lining (Q1 ),was affected by Q2/Q1 .(4)As the successful drainage of the release tunnel has great influence on the wa-ter pressure on the second lining,scheduled check and maintenance should be done during the operation of the release tunnel to ensure smooth drainage.The study can provide a reference for the design and operation of high water level karst tunnel.